ASN Wikibase Occurrence # 292573
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 9 March 2006 |
Time: | 17:30 LT |
Type: | Cessna 210 |
Owner/operator: | Cvl Enterprises LLC |
Registration: | N6540X |
MSN: | 57540 |
Year of manufacture: | 1960 |
Total airframe hrs: | 4156 hours |
Engine model: | Continental IO-470-E |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Jesup, Georgia -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Brunswick-Malcolm McKinnon Airport, GA (SSI/KSSI) |
Destination airport: | Atlanta-DeKalb Peachtree Airport, GA (PDK/KPDK) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed the Malcolm Mc Kinnon Airport (SSI), on an instrument cross-country flight to Peachtree DeKalb Airport. He leveled off at 6,000 feet, and noticed that the engine analyzer No. 2 cylinder light began to flicker, and shortly thereafter the low voltage light illuminated. The pilot contacted air traffic control personnel (ATC), and requested to return to SSI. After the request was made to return to SSI, the engine began to shake violently while making a loud "banging" noise and the propeller stopped. The pilot informed ATC of the emergency, and requested to divert to the nearest airport. ATC diverted the pilot to the Jesup-Wayne County Airport (JES). The pilot stated that he was unable to maintain altitude and crashed into a stand of trees 2 miles southeast of JES. The crankshaft was removed from the engine and sent to the National Transportation Safety Board, Office of Research and Engineering Materials Laboratory Division for further examination. Examination disclosed that the crankshaft was broken due to fatigue through the crank cheek between the No. 1 and No. 2 connecting rod journals. Review of the airplane logbooks revealed that on November 20, 1989, a gear up landing occurred. The propeller was removed and the crankshaft was run-out and found to be .0006 out of round. According to the Service Bulletin M84-16, which was in place at the time of the mishap, if any damage greater than "minor dressing of the propeller tips to correct the problem" occurs, a complete teardown must be performed. A teardown was not performed, and a serviceable propeller was reinstalled and the airplane returned to service. The logbooks revealed there were approximately 750 flight hours on the crankshaft before it failed.
Probable Cause: The loss of engine power due to the fatigue failure of the crankshaft, which resulted in a forced landing, and an in-flight collision with trees. A factor associated with the accident was the failure of other maintenance personnel to comply with the engine manufacturer's service bulletin following a previous mishap.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL06LA050 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB ATL06LA050
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 06:16 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation