Accident Joel H Johnson Rans S-6ES Coyote II N5196W,
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ASN Wikibase Occurrence # 292581
 
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Date:Sunday 5 March 2006
Time:16:45 LT
Type:Silhouette image of generic COY2 model; specific model in this crash may look slightly different    
Joel H Johnson Rans S-6ES Coyote II
Owner/operator:Dan Medlin
Registration: N5196W
MSN: 0492295
Year of manufacture:1994
Total airframe hrs:218 hours
Engine model:Rotax 582
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Cartersville, Georgia -   United States of America
Phase: Unknown
Nature:Training
Departure airport:Cartersville Airport, GA (KVPC)
Destination airport:Cartersville Airport, GA (KVPC)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The certified flight instructor (CFI) and student pilot were practicing takeoff training, pattern work, and approach to landing instruction. The CFI stated that after making a "touch and go", the engine began to "sputter" and was losing power. The airplane was 300 to 400 feet above the ground and about two thirds down runway-01.The CFI took control of the airplane and leveled it out in hopes that the engine would regain power. The engine stopped and the CFI made a forced landing in a field adjacent to the airport. The airplane collided with a ditch on touchdown and nosed over. The registered owner of the airplane stated, "The engine assembly was removed from the airframe and examined. The top spark plugs were removed. The electrodes were normal as depicted in the Rotax Maintenance Manual, and the proper gap was set. The oil and fuel lines were not breached. A visual fuel sample was taken and no contaminants were noted. The fuel system was intact and full of fuel. The in-line fuel filters were free of contaminants. The carburetors were inspected and no contaminants were noted. The electrical system was examined. A functional check of the electrical coils and lighting coils was completed. No anomalies were noted. Manually turning the engine checked the gearbox. The rotary valves were functional and compression appeared normal with rotation of the engine by hand. The engine head was removed and no damage was noted to the pistons, sleeves or rings. No determination was made pertaining to the loss of engine power."



Probable Cause: The loss of engine power during cruise flight for undetermined reasons, which resulted in an forced landing, on ground collision with a ditch, and nose over.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL06LA048
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB ATL06LA048

History of this aircraft

Other occurrences involving this aircraft
19 February 2015 N5196W Private 1 Rincon, PR sub
Ditching

Revision history:

Date/timeContributorUpdates
09-Oct-2022 06:27 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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