Accident Eurocopter France AS-350-B2 N911ES,
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ASN Wikibase Occurrence # 292668
 
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Date:Thursday 26 January 2006
Time:10:25 LT
Type:Silhouette image of generic AS50 model; specific model in this crash may look slightly different    
Eurocopter France AS-350-B2
Owner/operator:Private
Registration: N911ES
MSN: 2665
Year of manufacture:1992
Total airframe hrs:5997 hours
Engine model:Turbomeca Arriel 1D1
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Port Isabel, Texas -   United States of America
Phase: Unknown
Nature:Training
Departure airport:Harlingen, TX (78TS)
Destination airport:Port Isabel Cameron County Airport, TX (KPIL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The 5,591-hour helicopter flight instructor reported that he was on the second day of training of a newly hired 10,000-hour commercial helicopter rated pilot. After the pilot's first landing on Runway 03 (4,999-feet long by 150-feet wide asphalt-concrete runway), the flight instructor asked the pilot to perform an Emergency Medical Service (EMS) takeoff (as described in the company's operations manual), and then enter the local traffic pattern. The flight instructor stated that the EMS takeoff procedure began by the pilot bringing the helicopter to a three to five foot hover in order to conduct a power check prior to the application of takeoff power. While the helicopter was at a hover, the flight instructor initiated a hovering autorotation; the pilot immediately applied forward cyclic, and then pulled up on the collective. The flight instructor considered the pilot's flight control inputs to be excessive, resulting in a high sink rate and an undesirable helicopter attitude for touchdown. The instructor immediately took control of the helicopter and brought it back to a level attitude in an attempt to cushion the landing. The flight instructor stated that the main rotor RPM was low and most of the collective had been used to prevent a nose low impact. The helicopter then descended approximately one to two feet, impacting terrain in a level attitude and then bounced forward approximately four feet.

Probable Cause: The pilot's failure to maintain rotor RPM and his improper touchdown during a simulated hovering autorotation. A contributing factor was the flight instructor's delayed remedial action.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DFW06CA062
Status: Investigation completed
Duration: 2 months
Download report: Final report

Sources:

NTSB DFW06CA062

History of this aircraft

Other occurrences involving this aircraft
20 October 2013 N911ES Metro Aviation Inc 0 Madison, MS sub
Bird strike

Revision history:

Date/timeContributorUpdates
09-Oct-2022 07:31 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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