Accident Beechcraft 76 Duchess N6697N,
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ASN Wikibase Occurrence # 292678
 
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Date:Saturday 21 January 2006
Time:12:10 LT
Type:Silhouette image of generic BE76 model; specific model in this crash may look slightly different    
Beechcraft 76 Duchess
Owner/operator:Private
Registration: N6697N
MSN: ME-272
Total airframe hrs:4556 hours
Engine model:Lycoming O-360-A1G6D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Hinesville, Georgia -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Atlanta-DeKalb Peachtree Airport, GA (PDK/KPDK)
Destination airport:Hinesville, GA (2J2)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was completing an instrument cross-country flight when the accident occurred. Upon arrival at the destination airport, the pilot was cleared for a visual approach by air traffic control. The pilot stated that during the landing phase to runway 14, with a light right crosswind, he heard a popping noise after touchdown and the airplane veered left. The pilot initiated a go-around as the airplane departed the runway surface into the grass. The pilot reported that while attempting to clear trees, the stall warning horn sounded. He stated that he retracted the landing gear and then retracted the flaps. He reported that after flap retraction, the airplane's left wing dropped, and the airplane lost altitude and collided with trees. Witnesses stated that the airplane climbed steeply and then banked to the left. According to witnesses, the airplane leveled, then the nose pitched up, rolled left, and nosed down into the trees. The pilot received serious injuries and the airplane was destroyed by impact forces and a postimpact fire. A postaccident examination of the wreckage determined that the landing gear was down and locked. The tires were consumed by fire. Other than the 'popping” sound reported by the pilot several days after his initial statement, no mechanical problems were reported by the pilot or found during the postaccident examination of the airplane.

Probable Cause: The pilot's failure to maintain airspeed which resulted in an inadvertent stall and subsequent impact with trees.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL06CA037
Status: Investigation completed
Duration: 3 months
Download report: Final report

Sources:

NTSB ATL06CA037

Revision history:

Date/timeContributorUpdates
09-Oct-2022 07:37 ASN Update Bot Added

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