ASN Wikibase Occurrence # 292720
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Date: | Sunday 1 January 2006 |
Time: | 19:36 LT |
Type: | Piper PA-23-160 |
Owner/operator: | Private |
Registration: | N4370P |
MSN: | 23-1871 |
Year of manufacture: | 1960 |
Total airframe hrs: | 4071 hours |
Engine model: | Lycoming O-320 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Phenix City, Alabama -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Brooksville-Hernando County Airport, FL (KBKV) |
Destination airport: | Winder Airport, GA (WDR/KWDR) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot was on a visual flight rules cross country flight when he began encountering instrument conditions. The pilot continued into the instrument conditions for about 30 minutes before asking Atlanta Approach Control for directions to the nearest airport for landing. The controller directed the pilot to two different nearby airports but both were below minimums. The pilot informed the controller that he was low on fuel and needed to land as soon as possible. The controller directed the pilot to the Columbus Metropolitan Airport, Columbus, Georgia. The pilot told the controllers that he would attempt an Instrument approach. The pilot attempted four unsuccessful approaches with the controllers talking him through each approach. On the fifth approach, at five miles from the runway the pilot stated that both engine's quit due to fuel exhaustion. The pilot called "mayday" and during the forced landing the airplane collided with trees and the ground separating the right wing, half of the left wing, and coming to rest inverted. The pilot did not report any mechanical deficiencies with the airplane during the attempted approaches.
Probable Cause: The pilot's inadequate decision to continue VFR flight into IMC conditions, which resulted in a loss of engine power due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL06CA031 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB ATL06CA031
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 08:28 |
ASN Update Bot |
Added |
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