ASN Wikibase Occurrence # 292792
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Date: | Thursday 8 December 2005 |
Time: | 17:00 LT |
Type: | Cessna 152 |
Owner/operator: | Command Aircraft Inc., |
Registration: | N49815 |
MSN: | 15281335 |
Year of manufacture: | 1978 |
Engine model: | Lycoming O-235 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Key Largo, Florida -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Marathon-Florida Keys Airport, FL (MTH/KMTH) |
Destination airport: | Bunnell, FL (X47) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that he had been asked by the owner to ferry an airplane that had just been purchased, and further said that the airplane had been sitting in an area that had extensive flooding, which had occurred as a result of hurricanes that had affected the area. After conducting a preflight examination the pilot said he took off, and was in cruise flight at an altitude of 1,500 feet for about 15 minutes, when all of a sudden, without warning, the engine ceased operating. He said he was able to keep the engine operating through the use of the primer, but after a little while the engine ceased operating all together, and he ditched the airplane in the ocean. The pilot also said that he had experienced "several problems" with the FAA, and at the time of the accident flight, both his FAA private pilot certificate and his FAA airframe and powerplant mechanic certificate had been revoked. After recovery from the ocean an FAA inspector examined the airplane and it was to have extensive corrosion. The magnetos, carburetor and spark plugs had either been worn, severely fouled, or had corroded, and according to the inspector, due to the flooding, as well as the airplane having been ditched in the ocean, he was unable to determine its preaccident condition.
Probable Cause: A loss of engine power for undetermined reasons that resulted in the airplane being ditched into the ocean. Contributing to the accident was the pilot's operation of an airplane with known deficiencies due to it having sat in flooded waters.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA06LA026 |
Status: | Investigation completed |
Duration: | 2 years |
Download report: | Final report |
|
Sources:
NTSB MIA06LA026
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 09:11 |
ASN Update Bot |
Added |
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