Accident Piper PA-24-250 N7466P,
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ASN Wikibase Occurrence # 292821
 
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Date:Sunday 20 November 2005
Time:18:10 LT
Type:Silhouette image of generic PA24 model; specific model in this crash may look slightly different    
Piper PA-24-250
Owner/operator:
Registration: N7466P
MSN: 24-2657
Total airframe hrs:5596 hours
Engine model:Textron Lycoming O-540-A1D5
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Tucson, Arizona -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Tucson, AZ (57AZ)
Destination airport:Klamath Falls-Kingsley Field, OR (LMT/KLMT)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane landed hard during a forced landing following a loss of engine power in cruise flight. After a normal departure the airplane climbed to about 4,800 feet mean sea level (msl). The pilot noticed an audible difference in the engine operation, as if it were making intermittent pauses. As he was flying back to the airpark the engine continued to operate abnormally and began to make severe "popping" sounds. Despite the pilot's efforts, the engine failed to respond to his troubleshooting attempts and subsequently lost power. The airplane touched down about 1/3 down the runway, contacting the surface hard. A post-accident inspection preformed by a Federal Aviation Administration certificated mechanic who also holds an Inspection Authorization (IA) revealed that the mixture cable had disconnected at the carburetor. Specifically, the mixture linkage was separated where the cable adjoins the mixture control arm. The pilot and mechanic opined that the separation of the linkage would decrease the fuel supply and alter the fuel/air ratio, resulting in a subsequent loss of power. The airplane had last undergone an annual inspection 44 flight hours prior to the accident; the cable was last inspected at that time. The pilot stated that due to the location of the mixture cable, the mechanic would have to remove the cable from the throttle arm to inspect it in its entirety. The airplane's service manual states that during every 100-hour inspection the mechanic should inspect the mixture cable for, "travel and operating condition."

Probable Cause: the separation of the mixture cable at the carburetor control arm, which resulted in a loss of power, and maintenance personnel's inadequate inspection of the airplane during the last annual inspection.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX06LA044
Status: Investigation completed
Duration: 9 months
Download report: Final report

Sources:

NTSB LAX06LA044

History of this aircraft

Other occurrences involving this aircraft
10 April 1991 N7466P J & L Flying, Inc. 0 Casa Grande, AZ sub

Revision history:

Date/timeContributorUpdates
09-Oct-2022 09:34 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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