ASN Wikibase Occurrence # 293003
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Date: | Monday 26 September 2005 |
Time: | 12:46 LT |
Type: | Cessna A185F |
Owner/operator: | Private |
Registration: | N8548Q |
MSN: | 18503730 |
Year of manufacture: | 1979 |
Total airframe hrs: | 3415 hours |
Engine model: | Teledyne Continental IO-520-D |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Tracy, California -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Tracy Municipal Airport, CA (KTCY) |
Destination airport: | Albany Airport, OR (CVO/KCVO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the takeoff initial climb the engine experienced a partial loss of power and the landing gear collapsed during an ensuing off-airport forced landing in an open field. Upon arriving at the airport, the pilot conducted a preflight inspection, which included checking the fuel tanks for contamination. No discrepancies were noted with the preflight inspection, start-up, taxi to the active runway, or run-up. Shortly after takeoff the pilot reduced the throttle and revolutions per minute (rpm) to 25 inches of manifold pressure (MAP) and 2,500 rpm for best rate of climb. Shortly after that the pilot noticed that the climb performance was substandard and decaying, and the engine seemed to have a reduced power output. Due to the marginal climb performance and decaying power state of the engine, the pilot decided to land in an open field. During a turn to remain over the intended landing site, the engine started to misfire. Engine power continued to decay even though the throttle was full forward, mixture set at rich, and the fuel selector was selected to BOTH. While on downwind he noted obstructions at the end of his intended landing site. At the current rate of descent, he believed that the airplane would overrun the field and impact the obstructions. He lowered the flaps to 20 degrees and initiated a left 90-degree turn for a clearer area in which to land. During the flare, the left wing tip impacted the ground first, the airplane bounced, and when it touched down again, the right main landing gear collapsed. A post accident inspection and ground run of the engine was conducted by a Federal Aviation Administration inspector with no preimpact mechanical anomalies identified that would have precluded normal operation.
Probable Cause: loss of engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX05LA317 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB LAX05LA317
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 14:52 |
ASN Update Bot |
Added |
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