ASN Wikibase Occurrence # 293098
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Date: | Tuesday 6 September 2005 |
Time: | 17:25 LT |
Type: | Piper PA-28-161 |
Owner/operator: | Nassau Flyers Inc |
Registration: | N8270M |
MSN: | 28-8116045 |
Year of manufacture: | 1980 |
Total airframe hrs: | 11539 hours |
Engine model: | Lycoming O-320-D3G |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Babylon, New York -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Farmingdale-Republic Airport, NY (FRG/KFRG) |
Destination airport: | Farmingdale-Republic Airport, NY (FRG/KFRG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot leveled the airplane after takeoff, and encountered "a lot of roughness in the engine." The engine rpm fluctuated greatly, the entire airframe vibrated, and the windscreen became covered in oil. The pilot declared an emergency and attempted a return to the departure airport. The engine power continued to decrease, and the airplane could not maintain altitude, so the pilot selected a parking lot for landing. During the landing, the airplane cleared a vehicle in its path, touched down, overran the lot, and collided with two rows of bushes before it came to rest against a sand dune. Examination of the airplane revealed holes in the engine case in the area of the No. 1 exhaust tappet and the No. 3 exhaust tappet. Partial disassembly revealed that the No. 3 piston "split in half" at the oil control ring/piston ring journal, and the No. 1 exhaust valve tappet was broken. Maintenance records revealed that the engine had accumulated 771 hours beyond the manufacturer's recommended 2,000-hour time between overhaul.
Probable Cause: A broken piston and exhaust valve tappet which resulted in a total loss of engine power, and a forced landing to unsuitable terrain. A contributing factor was the failure of the operator to overhaul the engine at the manufacturer's recommended interval.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | IAD05LA133 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB IAD05LA133
Revision history:
Date/time | Contributor | Updates |
09-Oct-2022 16:02 |
ASN Update Bot |
Added |
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