ASN Wikibase Occurrence # 293994
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Date: | Saturday 19 March 2005 |
Time: | 17:36 LT |
Type: | Schweizer 269C |
Owner/operator: | Marpat Aviation |
Registration: | N61193 |
MSN: | S1593 |
Year of manufacture: | 1992 |
Total airframe hrs: | 1848 hours |
Engine model: | Lycoming HIO-360-D1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Leet, West Virginia -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | S. Charleston, WV (WV12) |
Destination airport: | Logan, WV (6L4) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While investigating a fire, the pilot noticed an "unusual vibration," and a "needle split" on the rpm gauge. The rotor speed began to decay and the engine speed began to increase. The pilot then entered an autorotation. The helicopter, impacted terrain, was substantially damaged, and a passenger was seriously injured. Examination of the drive train revealed that the main drive pinion, which drove both the main rotor assembly and the tail rotor drive shaft, had failed in fatigue that had initiated in the root of the first (most forward) engaged pinion thread. The failed pinion had been in service for 4,055.4 hours. Including the accident pinion, 10 instances of pinion failures were identified during the investigation. Times in service ranged from 261.5 to 4,243 hours. According to the manufacturer, life limits for the pinion ranged from 6,000 to 8,000 hours depending on application. As a result of this investigation, The FAA issued an SAIB alerting owners and operators of pending revisions to the inspection procedures for the pinion. The manufacturer revised its Handbook of Maintenance Instructions, to include the revised inspection procedures, and submitted design revisions to the FAA to make the part more robust.
Probable Cause: A fatigue fracture of the main transmission drive pinion. Also causal was the manufacturer's failure to remove the affected pinions from service during the period that transpired between the initial failures and the accident flight.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | IAD05LA046 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB IAD05LA046
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
10-Oct-2022 16:00 |
ASN Update Bot |
Added |
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