ASN Wikibase Occurrence # 294006
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 16 March 2005 |
Time: | 15:31 LT |
Type: | Cessna 152 |
Owner/operator: | |
Registration: | N64986 |
MSN: | 15281513 |
Year of manufacture: | 1978 |
Total airframe hrs: | 4455 hours |
Engine model: | Lycoming O-235 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Port Royal, Virginia -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Raleigh/Durham, NC (RDU |
Destination airport: | Clinton, MD (W32) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot departed into instrument meteorological conditions and initially encountered icing at 5,000 feet. He then descended the airplane to 3,000 feet, where about 30 minutes later the engine experienced roughness. After an application of carburetor heat, the engine smoothed and the pilot continued the flight. About 1 hour later, and at an altitude of 4,000 feet, the pilot noted the presence of mist, and that the temperature was slightly above freezing, and activated the pitot heat. Shortly thereafter the engine suddenly "quit," and the pilot performed a forced landing to a highway. During the landing rollout, both wings struck signs next to the highway and the airplane then veered off the highway and into a median. Following the accident, FAA inspectors asked the pilot to start the engine, and it ran for 30 seconds at idle rpm, until the pilot shut it down. During the recovery process, about 2 gallons of fuel were drained from the fuel tanks, and no indications could be found that either fuel tank had been compromised during the accident. The pilot stated that prior to the accident flight, he determined the amount of fuel onboard the airplane by estimating the fuel consumed on the previous flight.
Probable Cause: A loss of engine power due to the pilot's inadequate preflight planning which resulted in fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | IAD05LA045 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB IAD05LA045
Revision history:
Date/time | Contributor | Updates |
10-Oct-2022 16:11 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation