Accident Navion Navion H N2512T,
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ASN Wikibase Occurrence # 294024
 
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Date:Saturday 12 March 2005
Time:11:38 LT
Type:Silhouette image of generic NAVI model; specific model in this crash may look slightly different    
Navion Navion H
Owner/operator:Private
Registration: N2512T
MSN: NAV-4-2512T
Total airframe hrs:5093 hours
Engine model:Continental IO-520-B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Hubbard, Oregon -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Hubbard, OR (7S9)
Destination airport:McMinnville Municipal Airport, OR (KMMV)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot said, in a telephone interview, that he used a check-list to preflight the airplane, and he checked the fuel tanks for contamination. He said he started the engine with the fuel selector in the both position, and taxied with it in the left main position. He performed his engine run-up with the fuel selector in the right main position. The pilot said that as he took the active runway 02 for takeoff, he switched the fuel selector to the both position. Witnesses said that the airplane had just taken off, when the engine appeared to lose power. The pilot performed a forced landing into a Christmas tree farm. He was critically injured during the landing; he was not wearing shoulder harnesses. On June 21, 2005, the pilot submitted a written statement which said: "As I taxied to the departure end of Rwy 02 I cycled the fuel selector valve from L to R and back to Main with no interruption of engine operation." He further said that the airplane's engine run up was normal and the takeoff was normal until immediately after takeoff when the engine quit with no sputtering or surging. The engine mount was bent, the right wing, fuselage, and empennage were bent, wrinkled, and twisted. The engine was test run through its full power band. No preimpact engine or airframe anomalies, which might have affected the airplane's performance, were identified









Probable Cause: The total loss of engine power immediately after takeoff for undetermined reason.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA05FA061
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB SEA05FA061

Revision history:

Date/timeContributorUpdates
10-Oct-2022 16:23 ASN Update Bot Added

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