Accident Cessna T207A N207CC,
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ASN Wikibase Occurrence # 294075
 
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Date:Wednesday 23 February 2005
Time:16:45 LT
Type:Silhouette image of generic C207 model; specific model in this crash may look slightly different    
Cessna T207A
Owner/operator:
Registration: N207CC
MSN: 20700488
Total airframe hrs:10848 hours
Engine model:Continental IO-520F
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:West Palm Beach, Florida -   United States of America
Phase: Unknown
Nature:Private
Departure airport:West Palm Beach, FL (F45)
Destination airport:(F45)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that a remanufactured engine was installed and a post installation check flight was performed for about 15 minutes in the pattern. He landed and the maintenance facility did a post flight examination of the airplane for any discrepancies; none was observed. The pilot elected to conduct a local flight to break in the engine. The pilot did an engine run up, departure, and climb to 2500 feet, where he remained for a little over one hour. While descending to traffic pattern altitude, he reduced the throttle and the engine lost power. He then placed the throttle back to full power, turned on the electric fuel pump, checked the mixture was full rich, and attempted to restart the engine several times. The pilot then realized he would not make the runway and made an off airport landing, incurring substantial damage to the airplane. When the FAA inspector and the mechanics arrived at the scene they inspected the aircraft visually for fuel and found no fuel in the right tank and 11 gallons in the left. According to the pilot the fuel selector valve was on the right tank position at the time of engine failure. Examination of the fuel lines and fuel manifold revealed little fuel. The gascolator was about half full of fuel when removed. When fuel was drained from the right header tank very little fuel was observed. The engine was examined for a propeller strike and afterwards run on a test stand; no discrepancies were noted.

Probable Cause: The pilot's inadequate fuel management resulting in a loss of engine power due to fuel starvation and subsequent impact with an embankment during an emergency landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA05LA063
Status: Investigation completed
Duration: 1 year and 2 months
Download report: Final report

Sources:

NTSB MIA05LA063

History of this aircraft

Other occurrences involving this aircraft
17 January 1989 N6347H Courier Services Inc. 0 Page, AZ sub

Revision history:

Date/timeContributorUpdates
10-Oct-2022 16:59 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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