Accident Hughes OH-6A N8524Z,
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ASN Wikibase Occurrence # 295128
 
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Date:Tuesday 7 October 2003
Time:10:58 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes OH-6A
Owner/operator:U.s. Border Patrol Air Operations
Registration: N8524Z
MSN: 65-12933
Year of manufacture:1966
Total airframe hrs:14156 hours
Engine model:Allison C-20 B
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Eagle Pass, Texas -   United States of America
Phase: Unknown
Nature:Unknown
Departure airport:Del Rio International Airport, TX (DRT/KDRT)
Destination airport:Eagle Pass, TX (5T9)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The 2,363-hour pilot reported that he was maneuvering the helicopter at an altitude of 30 to 60 feet AGL, with 5 to 10 knots forward airspeed when the nose of the helicopter started to move to the right. The pilot corrected for this with the left pedal. The nose of the helicopter stopped momentarily then started moving back to the right and could not be stopped with full left pedal. The helicopter was spinning uncontrollably to the right and the engine and rotor RPM increased. The pilot tried to hold the helicopter level with the cyclic, lowered the collective, held full left pedal and started to retard the throttle when contact with the ground occurred. The helicopter came to rest on its left side. The pilot reported that the tail rotor was not turning when the helicopter hit the ground. Examination of the helicopter by the operator revealed that the aft segment of the tail rotor drive shaft, approximately 24 inches forward of the tail rotor gear box attach point, was separated. The reason for the separation was not determined.


Probable Cause: The failure of the aft segment of the tail rotor drive shaft for undertermined reasons. A contibuting factor was the lack of suitable terrain for the foced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW04TA012
Status: Investigation completed
Duration: 5 months
Download report: Final report

Sources:

NTSB FTW04TA012

Revision history:

Date/timeContributorUpdates
12-Oct-2022 18:19 ASN Update Bot Added

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