Accident Mooney M20D N6619U,
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ASN Wikibase Occurrence # 295330
 
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Date:Sunday 24 August 2003
Time:10:27 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20D
Owner/operator:Private
Registration: N6619U
MSN: 114
Year of manufacture:1963
Engine model:Lycoming O-360
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Hood River, Oregon -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Hood River, OR (4S2)
Destination airport:Eugene Airport, OR (EUG/KEUG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot's father (right seat), a commercial pilot with more than 2,000 hours in the accident aircraft, reported that the engine ran smoothly on the ground and an RPM check prior to takeoff yielded 2600 RPM. The takeoff roll on the 3,040-foot long asphalt runway seemed long with less than normal power to the flying pilot (left seat). The aircraft was rotated at 65 knots but settled back to the runway at which time the right seat pilot took control and established a shallow climb rate toward the rising terrain west of the airport. Both pilots felt that an aborted takeoff would result in an overrun into a grassy area containing vehicles and pedestrians. The flying pilot (right seat) then banked to avoid a large tree and the aircraft settled into the treetops eventually coming to rest inverted in a bog. Post-crash examination and test run of the engine revealed that the number one cylinder could develop no more than 25-35 pounds of compression. Further examination revealed the number one cylinder intake seat had dropped down out of its normally seated position at an angle preventing the valve from seating evenly during the compression stroke.

Probable Cause: A power loss due to a mis-seated intake valve on the #1 cylinder resulting in leakage during the compression stroke and low compression. Contributing factors were the rising terrain and trees.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA03LA176
Status: Investigation completed
Duration: 9 months
Download report: Final report

Sources:

NTSB SEA03LA176

Revision history:

Date/timeContributorUpdates
13-Oct-2022 07:10 ASN Update Bot Added

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