Accident Van's RV-6A N272JT,
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ASN Wikibase Occurrence # 295458
 
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Date:Saturday 26 July 2003
Time:10:30 LT
Type:Silhouette image of generic RV6 model; specific model in this crash may look slightly different    
Van's RV-6A
Owner/operator:Private
Registration: N272JT
MSN: 23975
Total airframe hrs:102 hours
Engine model:Lycoming IO-360-A1A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Wenatchee, Washington -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Wenatchee-Pangborn Field, WA (EAT/KEAT)
Destination airport:Chelan, WA (S10)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:

The experimental aircraft had just departed runway 30, and was about 400 feet above the ground, when it experienced a complete loss of engine power. The pilot then turned toward an empty field where he was going to attempt an engine-out forced landing, but he was unable to reach the field, and the aircraft impacted an orchard of young apple trees just short of the selected field. A post-accident inspection of the aircraft revealed that the screw holding the valve retaining faceplate on the Airflow Performance Purge Valve Assembly had come loose, allowing the valve mechanism to separate from its housing. It was further determined that the subject retaining screw had not been re-safetied after the builder removed the manufacturer-installed safety wire in order to change the angular configuration of the purge valve/flow divider assembly. A review of the Airflow Performance Installation and Service Manual revealed a narrative section stating that if removal of the valve is necessary, to make sure that the purge valve stop/faceplate screw is re-safetied.



Probable Cause: Fuel starvation following the separation of a purge valve assembly as a result of the builders failure to re-safety the face retaining/stop screw on the fuel vapor purge valve after the safety wire on the subject screw was removed in order to change the angular mounting position of the valve. Factors include an apple orchard near the edge of the field that pilot was trying to glide to.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA03LA154
Status: Investigation completed
Duration: 5 months
Download report: Final report

Sources:

NTSB SEA03LA154

Revision history:

Date/timeContributorUpdates
13-Oct-2022 08:45 ASN Update Bot Added

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