Accident Helio H800 N4035K,
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ASN Wikibase Occurrence # 295753
 
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Date:Saturday 7 June 2003
Time:14:30 LT
Type:Silhouette image of generic COUR model; specific model in this crash may look slightly different    
Helio H800
Owner/operator:Schmidt Aviation, Inc.
Registration: N4035K
MSN: H-6
Total airframe hrs:918 hours
Engine model:Lycoming IO-720-A1B
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Cody, Wyoming -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Cody-Yellowstone Regional Airport, WY (COD/KCOD)
Destination airport:Soldier's Bar, ID
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported, "A few seconds after becoming airborne, oil began splashing onto the windscreen and boiling out of the cowling around the oil cap access door." The pilot decided to land immediately. The pilot said he maintained runway heading to gain some altitude, approximately 300 to 400 feet above ground level (agl). He said he flew beyond the departure end of the runway and then made a 180-degree turn back to the airport. The pilot said he lowered flaps and began his descent. At approximately 150 feet agl, the pilot said he encountered "a severe downdraft, which caused the airplane to sink at a rapid rate. Although I immediately added full power, I was unable to overcome the downdraft." The airplane impacted terrain off the departure end of the runway causing substantial damage to the wings, fuselage, undercarriage, and vertical stabilizer. An examination of the airplane showed the oil cap off and the dip stick out. The examination also showed oil streaks around the oil filler door, across the top of the engine cowling, and on the inside of the engine cowling. The weather conditions approximately 5 minutes after the accident were clear skies, 10 miles visibility, and winds at 130 degrees magnetic at 5 knots.

Probable Cause: the pilot's improper preflight planning and his failure to maintain aircraft control when returning to the airport. Factors contributing to the accident were the oil leak, the attempted precautionary landing, and the downdraft.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN03LA098
Status: Investigation completed
Duration: 5 months
Download report: Final report

Sources:

NTSB DEN03LA098

Revision history:

Date/timeContributorUpdates
13-Oct-2022 12:29 ASN Update Bot Added

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