Accident Piper PA-32-260 N3921W,
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ASN Wikibase Occurrence # 295837
 
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Date:Friday 23 May 2003
Time:06:30 LT
Type:Silhouette image of generic PA32 model; specific model in this crash may look slightly different    
Piper PA-32-260
Owner/operator:Private
Registration: N3921W
MSN: 32-868
Year of manufacture:1967
Engine model:Lycoming O-540-E4B5
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Fort Meade, Florida -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Fort Meade, FL
Destination airport:Marsh Harbour-Leonard M. Thompson International Airport (MHH/MYAM)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that he performed weight and balance calculations before the flight by asking the passenger's their weights and estimating the weights of the passenger's bags. He calculated the airplane was in center of gravity and weight limits. He performed a preflight inspection of the airplane, no discrepancies were noted. Before takeoff from the 3,000-foot-grass strip with approximately 4-inch tall grass, he performed an engine run-up with no discrepancies noted. He lowered the flaps to 10 degrees and initiated a short/soft field takeoff; he applied full power while rolling onto the runway. The engine responded and he estimated the airplane became airborne approximately 3/4 down the runway. While airborne at 20 feet above ground level, the airplane, "...stalled came back down and began sliding." The airplane traveled through 3 fences before coming to rest. He further stated he expected the airplane should have become airborne about 1/2 way down the runway, and there was no mechanical failure or malfunction. The airplane was recovered and no repairs to the engine or its systems were performed. With FAA oversight, the engine was started and operated to 2,000 rpm. Safety concerns prevented operation to a higher rpm; no discrepancies were noted during the engine run. The engine was operated with the fuel selector positioned to the tank that had been selected for takeoff (right main fuel tank).

Probable Cause: Thew failure of the pilot to abort the takeoff after travelling past the estimated point of liftoff, and failure of the pilot to maintain airspeed during the initial climb resulting in inadvertent stall and uncontrolled descent with subsequent impact onto the runway.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA03LA111
Status: Investigation completed
Duration: 11 months
Download report: Final report

Sources:

NTSB MIA03LA111

Revision history:

Date/timeContributorUpdates
13-Oct-2022 13:28 ASN Update Bot Added

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