ASN Wikibase Occurrence # 296123
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Date: | Friday 14 March 2003 |
Time: | 17:30 LT |
Type: | Piper PA-28-180 |
Owner/operator: | Ed Schlosser |
Registration: | N5264L |
MSN: | 28-4562 |
Year of manufacture: | 1967 |
Total airframe hrs: | 4514 hours |
Engine model: | Lycoming L-11959-36A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bonham, Texas -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Meridian-Key Field, MS (MEI/KMEI) |
Destination airport: | Sherman, TX (F39) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane was painted at a maintenance facility prior to being delivered to its new owner. A private pilot was contacted by the maintenance facility to ferry the airplane. The 90-hour pilot reported that she flew on the right tank for the first 30 minutes of the flight, changing the fuel selector every hour thereafter. The pilot added that to switch the fuel selector, she had to move her left leg and look at the fuel selector every time she switched tanks since she was unable to feel the detent to make sure the selector was in the proper position. About 10 minutes after leveling-off at 3,000 feet, while 25-nautical miles from her next refueling stop, the pilot reported a rough running engine, followed by a complete loss of engine power. The airplane was too low to make the field and the airplane collided with matured trees just short of the selected field. The engine was removed from the airframe and after installing a test propeller, the engine was successfully ran to 2,400 RPMs. Further examination of the fuel system revealed that the fuel selector placard (Piper P/N 63832) was the correct type for this airplane; however, the pointer (handle) was not the correct type for this model aircraft. The installed pointer(handle) was to be used on later models of the airplane (s/n 28-7105001 and up). The installed pointer (handle) was found to have the fuel valve shaft indexed differently than the correct pointer (Piper P/N 63949) for this model, and the pointer would not properly align with the placard. An unknown installer appeared to have re-drilled the holes in the placard and cocked it about 45 degrees so the pointer would align with the placard and the detents in the valve.
Probable Cause: The loss of engine power due to fuel starvation as result of the unapproved fuel selector valve handle installed on the aircraft by an unknown person. A contributing factor was the lack of suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW03LA113 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB FTW03LA113
Revision history:
Date/time | Contributor | Updates |
13-Oct-2022 16:48 |
ASN Update Bot |
Added |
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