ASN Wikibase Occurrence # 296142
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Date: | Saturday 8 March 2003 |
Time: | 12:00 LT |
Type: | Cessna 172H |
Owner/operator: | |
Registration: | N275SW |
MSN: | 17255491 |
Year of manufacture: | 1966 |
Total airframe hrs: | 6168 hours |
Engine model: | Continental O-300-D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Callao, Missouri -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Callao, MO (KPVT) |
Destination airport: | Macon, MO (K89) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The aircraft was substantially damaged during a forced landing at a private airstrip. According to the pilot's statement, shortly after departure, approximately 3 miles west of the airstrip, the engine "started cutting out." He reported that he applied carburetor heat and checked the mixture, however, the engine performance did not improve. At that point, he decided to return to the local airstrip. The pilot stated: "Approximately 1/2 mile away I slowed down and added 20 degrees of flaps. As I approached the threshold end at a heading of 090 degrees, I applied more flaps. The airplane stayed in ground [effect] and didn't land until about 2/3 of the way down the runway. Upon touchdown I took out all flaps as the airplane slid down the grass/muddy runway. The airplane slid off the end of the runway with the nose wheel striking a gravel road and breaking off. The airplane then flipped over coming to rest upside down in the road ditch." The pilot reported that he decided to approach straight-in, for a downwind landing, due to the lack of available power, as well as the rising terrain and two sets of power lines east of the airstrip. He noted that he was slightly fast on final approach. According to the pilot, his preflight weather briefing advised of winds from 240 degrees at 14 knots. Winds reported 20nm north of the accident site were from 330 degrees at 17 knots. During a post accident examination, no compression was obtained on engine cylinder 2. The number 2 cylinder was removed and the cylinder and piston were inspected. The bottom edge of the number 2 piston head was eroded and burned. The damage extended past the piston rings and included a hole in the side of the piston. In addition, the side of the piston as well as the cylinder wall, exhibited scoring in the direction of piston travel. The piston rings were broken. The condition of the piston was consistent with pre-ignition.
Probable Cause: A loss of engine power due to the erosion of the number 2 piston, resulting in loss of compression on that cylinder. Contributing factors were the tailwind, the muddy runway condition, and the roadway and ditch.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI03LA082 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB CHI03LA082
Revision history:
Date/time | Contributor | Updates |
13-Oct-2022 17:05 |
ASN Update Bot |
Added |
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