Accident Aeronca 7AC N1648E,
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ASN Wikibase Occurrence # 296148
 
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Date:Friday 7 March 2003
Time:17:45 LT
Type:Silhouette image of generic CH7A model; specific model in this crash may look slightly different    
Aeronca 7AC
Owner/operator:Carole Anne Taylor
Registration: N1648E
MSN: 7AC-5213
Total airframe hrs:2391 hours
Engine model:Continental A65-8
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Gordo, Alabama -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Tuscaloosa Regional Airport, AL (TCL/KTCL)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During cruise flight a "bump" was felt under the pilot's seat, then the airplane pitched up erratically and became difficult to control. The pilot selected an open field and executed an emergency landing. The airplane came to rest in a pond. The pilot reported that the crankshaft sheared behind the propeller flange and in front of the crankcase. Examination of the airplane on site revealed that one of the propeller blades separated at the flange, there was substantial damage to the nose bowl cowling due to the airplane nosing over into the pond. The firewall was bent slightly rearward at the base and there was also water damage to the wing spar. Further examination of the partial crankshaft recovered, revealed that the separation had occurred between the oil slinger and the propeller mounting flanges leaving a fracture face. The fracture face displayed arced crack arrest marks, consistent with fatigue propagation. The arcing of the crack arrest marks indicated that the fatigue origin was located further forward, towards the propeller-mounting flange on the unrecovered portion of the crankshaft.

Probable Cause: Fatigue failure of the crankshaft.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL03LA059
Status: Investigation completed
Duration: 3 years and 3 months
Download report: Final report

Sources:

NTSB ATL03LA059

Revision history:

Date/timeContributorUpdates
13-Oct-2022 17:06 ASN Update Bot Added

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