ASN Wikibase Occurrence # 296218
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Date: | Saturday 8 February 2003 |
Time: | 10:15 LT |
Type: | Beechcraft A23 |
Owner/operator: | Cascade Wings LLC |
Registration: | N2392W |
MSN: | MA-7 |
Total airframe hrs: | 1653 hours |
Engine model: | Lycoming IO-360-A2B |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fort Klamath, Oregon -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Redmond-Roberts Field, OR (RDM/KRDM) |
Destination airport: | Chiloquin, OR (2S7) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that during descent for landing, the engine started to "knock" and "shutter." About 15 seconds later a "significant noise" was heard and oil and smoke began to come out of the engine cowling. The pilot initiated a forced landing to an open field. During the landing roll, the aircraft traveled over a ditch, which sheared off the nose gear. During the post-accident engine inspection, oil was visible on the bottom engine cowling and oil was streaked along the bottom of the fuselage from the engine to the tail. A large hole was noted to the top left side of the crankcase as well as a hole in the bottom left side between cylinders two and four. The number two rod end cap was missing as well as the bolts and nuts. Severe heat distress was noted on the number two connecting rod end and to the associated crankshaft rod journal. All oil passages were clear. The number two bearing was missing. Fragments of connecting rod and bearing material was found in the oil sump. The remaining connecting rods were intact with no evidence of heat distress noted. All oil lines were intact and connections were tight. No evidence of an oil leak was noted.
Probable Cause: The separation of the rod end cap from the connecting rod for an undetermined reason during the descent for landing. The ditch was a factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA03FA038 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB SEA03FA038
Revision history:
Date/time | Contributor | Updates |
13-Oct-2022 17:59 |
ASN Update Bot |
Added |
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