ASN Wikibase Occurrence # 297687
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Date: | Sunday 6 January 2002 |
Time: | 12:30 LT |
Type: | Cessna 414A Chancellor |
Owner/operator: | Mid Continent Aire Ltd |
Registration: | N6560C |
MSN: | 414A0013 |
Year of manufacture: | 1977 |
Total airframe hrs: | 2570 hours |
Engine model: | Continental TSIO-520N |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Sturgis, Michigan -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Sturgis-Kirsch Municipal, MI (IRS/KIRS) |
Destination airport: | New Braunfels Regional Airport, TX (KBAZ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot attempted a single engine missed approach to the departure airport following a loss of right engine power during the departure climb phase of flight. The pilot reported that he was high on the approach and then feathered the propeller when the missed approach was executed. Instrument meteorological conditions prevailed at the time of the accident. Graphical performance data for the airplane shows a positive climb rate, at field conditions, of approximately 340 fpm based upon the airplanes checklist configuration for single engine flight. The data also shows a loss of single engine climb performance of 400 fpm if the propeller is not feathered in addition to a loss of 200 fpm with a flap setting of 15 degrees. Examination of the right engine revealed that the oil return line from the turbocharger to the scavenge oil pump was disconnected and did not exhibited stripping of the connectors threads. Removal of the engine's oil pan also revealed the presence of metallic debris. Engine logbook information indicates that the last recorded maintenance performed on the engine was the engine's installation 31.7 hours prior to the accident.
Probable Cause: the inadequate in-flight emergency planning/decision, the checklist not followed and excessive approach altitude by the pilot. Contributing factors were the loose oil return line and weather.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI02LA060 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB CHI02LA060
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 07:15 |
ASN Update Bot |
Added |
16-Nov-2022 23:33 |
Ron Averes |
Updated [Aircraft type, Narrative] |
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