ASN Wikibase Occurrence # 297785
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Friday 30 August 2019 |
Time: | 07:37 LT |
Type: | Hall Kitfox |
Owner/operator: | |
Registration: | N87TJ |
MSN: | 158 |
Year of manufacture: | 1988 |
Total airframe hrs: | 502 hours |
Engine model: | Jabiru 2200 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Nampa, Idaho -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Caldwell Industrial Airport, ID (KEUL) |
Destination airport: | Nampa-KMAN, ID (MAN/KMAN) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that, during takeoff in the experimental, amateur-built, tailwheel-equipped airplane, he experienced a hard shimmy before liftoff. Following an uneventful flight, the pilot landed the airplane onto the main landing gear. When the tailwheel touched down, the airplane immediately became uncontrollable and unresponsive. The airplane was rolling toward the right side of the runway and the pilot applied the brakes in an attempt to slow the airplane. The propeller contacted the runway surface before the airplane exited the runway, nosed over, and came to rest inverted.
The pilot reported that, about 6 to 8 weeks before the accident, the owner installed a larger tailwheel on the airplane. The original tailwheel was about 3 or 4 inches in diameter. The new tailwheel was about 6 inches in diameter.
A postaccident examination of the airplane revealed that the airplane was equipped with a 1 1/4-inch tailwheel leaf spring. The new tailwheel was designed for a 1 1/2-inch tailwheel leaf spring; therefore, a shim would have been required to ensure proper installation. In addition, a longer bolt would be needed to ensure that the bolt would properly secure within the locking nut. The examination revealed that the bolt was still present in the leaf spring, but the locking nut was not present and was not located along the runway. The washer was found underneath the tail, and there were no indications that a shim was installed. The bolt was removed from the leaf spring and measured; it was not long enough to reach the locking portion of the locking nut.
Since the bolt was not long enough to reach the locking portion of the locking nut, it is likely that the nut vibrated loose during normal operations, which caused excessive play in the tailwheel during landing.
Probable Cause: The owner's improper installation of the tailwheel, which resulted in the pilot's inability to maintain directional control during landing as a result of severe tailwheel vibrations.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR19TA248 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB WPR19TA248
Location
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 08:33 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation