ASN Wikibase Occurrence # 297878
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 30 April 2019 |
Time: | 18:00 LT |
Type: | Cessna 172 |
Owner/operator: | |
Registration: | N3031U |
MSN: | 17250631 |
Year of manufacture: | 1963 |
Total airframe hrs: | 2562 hours |
Engine model: | Lycoming O-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Wasilla, Alaska -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | Wasilla Airport, AK (WWA/PAWS) |
Destination airport: | Wasilla Airport, AK (WWA/PAWS) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor reported that, during the preflight inspection, he asked the student pilot, who was the owner of the airplane, how much fuel was onboard the airplane and that the student replied that there was enough fuel for about 3 hours of flight. He added that, during the flight, he became concerned about the fuel level because he saw that the right fuel gauge needle displayed "little movement." After a brief conversation with the student about the fuel burn, the instructor decided to return to the airport.
The student stated that he visually checked the fuel tanks during the preflight and estimated that there was about 1/2 tank (19 gallons), which was enough for about 2.5 hours of flight based on a fuel burn of 7.5 gph. The student reported that, during the flight, the instructor commented that the fuel gauge looked low and that he responded that it was working "intermittently," at which point, the instructor decided to return to the airport.
The student reported that, about 5 nautical miles from the airport, the airplane "ran out of fuel at 3,000 ft MSL [mean sea level]." Subsequently, the instructor landed the airplane on a road, and the right wing struck a power line pole.
The airplane sustained substantial damage to the right wing.
Probable Cause: The flight instructor's failure to verify the fuel level, which resulted in a total loss of engine power due to fuel exhaustion and a subsequent forced landing and collision with a power line pole. Contributing to the accident was the student pilot's inadequate preflight fuel planning.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA19CA236 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB GAA19CA236
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 09:50 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation