ASN Wikibase Occurrence # 297917
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 23 December 2018 |
Time: | 15:10 LT |
Type: | Cessna 182G Skylane |
Owner/operator: | |
Registration: | N3120S |
MSN: | 18255620 |
Year of manufacture: | 1964 |
Total airframe hrs: | 5878 hours |
Engine model: | Continental O-470-R |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Norwood, Colorado -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Nucla-Hopkins Field, CO (KAIB) |
Destination airport: | Nucla-Hopkins Field, CO (KAIB) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was conducting a personal flight. During the flight, he monitored the carburetor temperature gauge and used full, partial, and no carburetor heat settings as appropriate. While landing at his private, high-elevation airport, he initially had partial carburetor heat selected but then turned it off as he typically did to preclude ingestion of unfiltered air into the engine while landing on a dirt runway. During the approach, the airplane drifted left of the runway, so the pilot decided to go around. He advanced the engine power slightly, but the engine did not respond. He then advanced the engine power to full, but the engine still did not respond. The pilot then conducted a steep right turn and applied right rudder to land the airplane on the runway and avoid trees. He was not certain if the airplane stalled, but the right wingtip contacted the ground, and the airplane "pancaked" on the runway. The airplane sustained substantial damage to the fuselage and both wings.
After the accident, the pilot stated that he did not 'adequately†clear the carburetor during the approach and that it was possible the carburetor had "iced up" during the descent. However, the temperature and dew point at the time of the accident put the airplane outside of conditions conducive for icing; therefore, it is unlikely that carburetor accumulated icing. Thus, the reason for the loss of engine power could not be determined based on the available evidence.
Probable Cause: The partial loss of engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA061 |
Status: | Investigation completed |
Duration: | 2 years and 4 months |
Download report: | Final report |
|
Sources:
NTSB CEN19LA061
Location
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 10:24 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation