ASN Wikibase Occurrence # 297937
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Date: | Friday 12 October 2018 |
Time: | 12:04 LT |
Type: | Grumman American AA-5B Tiger |
Owner/operator: | |
Registration: | N81383 |
MSN: | AA5B-0522 |
Year of manufacture: | 1977 |
Engine model: | Lycoming O-360-A4K |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Refugio, Texas -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Fredericksburg, TX (TS36) |
Destination airport: | Refugio-Rooke Field, TX (KRFG) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was conducting a personal cross-country flight when he became lost. The pilot reported that he did not understand how to navigate using the GPS that was installed in the airplane before the flight. Instead of continuing to the southeast toward the intended destination, the pilot turned south for the remainder of the flight. After flying for about 1.5 hours, the pilot became concerned about how much fuel remained and decided to land to refuel. The pilot stated that the airplane had a total loss of engine power while in the airport traffic pattern, and that he did not maintain adequate airspeed, which resulted in an aerodynamic stall during the turn from the base leg to final. The airplane sustained substantial damage to the fuselage and empennage during impact.
Examination of the airplane revealed no fuel in the left fuel tank, about 7 gallons of fuel in the right fuel tank, and less than 2 fluid ounces of combined fuel from the electric boost pump, the fuel line to the carburetor, and the carburetor fuel bowl. The pilot reported that the fuel selector valve was positioned to the left fuel tank when the loss of engine power occurred. The loss of engine power was likely due to fuel starvation.
Probable Cause: The pilot's improper inflight fuel management, which resulted in a total loss of engine power due to fuel starvation and the pilot's failure to maintain adequate airspeed, which resulted in the airplane exceeding its critical angle of attack and an aerodynamic stall at a low altitude.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN19LA007 |
Status: | Investigation completed |
Duration: | 2 years and 10 months |
Download report: | Final report |
|
Sources:
NTSB CEN19LA007
Location
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 10:43 |
ASN Update Bot |
Added |
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