ASN Wikibase Occurrence # 298020
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Date: | Thursday 10 May 2018 |
Time: | 07:30 LT |
Type: | Cub Crafters CC19 |
Owner/operator: | 82xcub LLC. |
Registration: | N82XC |
MSN: | CC19-0018 |
Year of manufacture: | 2017 |
Total airframe hrs: | 30 hours |
Engine model: | Lycoming O-360-C1G |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mesa, Arizona -
United States of America
|
Phase: | Landing |
Nature: | Ferry/positioning |
Departure airport: | Phoenix-Deer Valley Airport, AZ (DVT/KDVT) |
Destination airport: | Phoenix-Deer Valley Airport, AZ (DVT/KDVT) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:According to the pilot, he was seated in the front seat of the tandem-seat, tailwheel-equipped airplane and made a three-point landing and applied full aft stick pressure once the tailwheel was on the ground. He could not recall the airspeed, but the airplane abruptly veered to the left. The right main landing gear (MLG) collapsed, and subsequently, the the right wing struck the ground.
The pilot-rated passenger, who was a flight instructor, reported that the purpose of the flight was to perform a prebuy inspection for the pilot. He reported that there was a slight crosswind from the left about 3 knots during the three-point landing, and the stall warning horn activated. He described the landing as "perfect," but during the landing roll, the airplane veered hard left and ground looped.
The Federal Aviation Administration aviation safety inspector who examined the airplane after the accident determined that the right MLG wheel assembly "folded under the end of the gear leg and then separated." The airplane manufacturer examined the wheel assembly and reported that "an extreme sideload on the right tire caused the subsequent cascading failure of the right wheel and brake assembly," which likely resulted from the ground loop.
The METAR at the accident airport reported that, about the time of the accident, the wind was from 180° at 7 knots. The pilot landed on runway 22L.
Probable Cause: The pilot's failure to maintain directional control of the airplane during the landing roll.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | GAA18CA272 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB GAA18CA272
Location
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 11:57 |
ASN Update Bot |
Added |
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