ASN Wikibase Occurrence # 298091
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Date: | Saturday 16 December 2017 |
Time: | 13:20 LT |
Type: | Cessna 152 |
Owner/operator: | Flying Academy Miami |
Registration: | N95550 |
MSN: | 15285918 |
Year of manufacture: | 1984 |
Total airframe hrs: | 10264 hours |
Engine model: | Lycoming O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Everglades City, Florida -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Miami Executive Airport, FL (TMB/KTMB) |
Destination airport: | Venice Municipal Airport, FL (VNC/KVNC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that while in level cruise flight on the personal flight, he adjusted the throttle and mixture controls. Shortly after, the engine lost total power. Emergency engine procedures did not restore engine power, and the pilot selected a nearby airport for a forced landing. During the subsequent emergency landing, the airplane struck a perimeter fence before impacting the ground just short of the runway, which resulted in substantial damage to the fuselage. A postaccident engine examination revealed that when the mixture control was manipulated, the cable moved, but the mixture arm on the carburetor did not move. When the fiber lock nut that attached the mixture cable to the mixture arm was tightened, the mixture linkage operated normally. The engine was then started and operated at various power settings. Given the absence of mechanical issues other than the loose mixture control fiber lock nut, it is likely that the mixture linkage became loose and the mixture control arm vibrated to the lean direction, which resulted in the mixture being too lean and the engine losing total power.
Probable Cause: The loose nut connecting the mixture control cable to the mixture control arm, which resulted in the pilot's inability to control the mixture and the subsequent total loss of engine power.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ERA18LA050 |
Status: | Investigation completed |
Duration: | 2 years and 5 months |
Download report: | Final report |
|
Sources:
NTSB ERA18LA050
Location
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 12:55 |
ASN Update Bot |
Added |
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