Fuel exhaustion Accident Mooney M20C N6753U,
ASN logo
ASN Wikibase Occurrence # 298274
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Sunday 18 November 2001
Time:13:10 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20C
Owner/operator:Private
Registration: N6753U
MSN: 2475
Year of manufacture:1963
Total airframe hrs:3487 hours
Engine model:Textron Lyc. O-360-A1D
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:High Springs, Florida -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Alabaster-Shelby County Airport, AL (KEET)
Destination airport:Gainesville-J R Alison Municipal Airport, FL (GNV/KGNV)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot stated that the aircraft was in cruise flight at an altitude of 7,000 feet, when all of a sudden the engine ceased operating. He further stated that he then engaged the fuel boost pump, and switched to the left fuel tank, and engine power was restored, but about 10 seconds after power had been restored, the engine ceased operating again. He said he again switched tanks, but the engine failed to operate a second time, and he ended up making a forced landing to a field. The pilot later stated to the NTSB that the reason the engine ceased operating was due to fuel exhaustion. According to the pilot, his wife, a passenger on the flight, had ordered fuel at Shelby County Airport in Alabaster, Alabama, prior to them departing on the flight, but the fuel had not been provided. In addition, an employee at the Shelby County Airport stated that fuel had been ordered for N6753U, but the linesman had forgotten the order, and that no fuel had been placed in the accident aircraft's fuel tanks, as was requested. An FAA Inspector who conducted a postaccident examination of the aircraft, said that during his investigation of the accident aircraft, he found no breaches to fuel system, and that all aircraft fuel tanks were "bone dry."

Probable Cause: The pilot's improper preflight planning/preparation and failure to ensure sufficient fuel was available to complete the flight, which resulted in fuel exhaustion, a forced landing, and damage to the aircraft when it collided with a fence during the landing rollout.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA02LA020
Status: Investigation completed
Duration: 3 months
Download report: Final report

Sources:

NTSB MIA02LA020

Revision history:

Date/timeContributorUpdates
15-Oct-2022 16:06 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org