ASN Wikibase Occurrence # 298274
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Date: | Sunday 18 November 2001 |
Time: | 13:10 LT |
Type: | Mooney M20C |
Owner/operator: | Private |
Registration: | N6753U |
MSN: | 2475 |
Year of manufacture: | 1963 |
Total airframe hrs: | 3487 hours |
Engine model: | Textron Lyc. O-360-A1D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | High Springs, Florida -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Alabaster-Shelby County Airport, AL (KEET) |
Destination airport: | Gainesville-J R Alison Municipal Airport, FL (GNV/KGNV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that the aircraft was in cruise flight at an altitude of 7,000 feet, when all of a sudden the engine ceased operating. He further stated that he then engaged the fuel boost pump, and switched to the left fuel tank, and engine power was restored, but about 10 seconds after power had been restored, the engine ceased operating again. He said he again switched tanks, but the engine failed to operate a second time, and he ended up making a forced landing to a field. The pilot later stated to the NTSB that the reason the engine ceased operating was due to fuel exhaustion. According to the pilot, his wife, a passenger on the flight, had ordered fuel at Shelby County Airport in Alabaster, Alabama, prior to them departing on the flight, but the fuel had not been provided. In addition, an employee at the Shelby County Airport stated that fuel had been ordered for N6753U, but the linesman had forgotten the order, and that no fuel had been placed in the accident aircraft's fuel tanks, as was requested. An FAA Inspector who conducted a postaccident examination of the aircraft, said that during his investigation of the accident aircraft, he found no breaches to fuel system, and that all aircraft fuel tanks were "bone dry."
Probable Cause: The pilot's improper preflight planning/preparation and failure to ensure sufficient fuel was available to complete the flight, which resulted in fuel exhaustion, a forced landing, and damage to the aircraft when it collided with a fence during the landing rollout.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA02LA020 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB MIA02LA020
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 16:06 |
ASN Update Bot |
Added |
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