ASN Wikibase Occurrence # 298305
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Date: | Friday 9 November 2001 |
Time: | 18:49 LT |
Type: | Cessna 210K |
Owner/operator: | Private |
Registration: | N8232M |
MSN: | 210-59232 |
Engine model: | Continental IO-520-L |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | North Las Vegas, Nevada -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Las Vegas-North Las Vegas Airport, NV (VGT/KVGT) |
Destination airport: | Lancaster-William J Fox Airport, CA (WJF/KWJF) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On the first flight following an annual inspection, in night, visual meteorological conditions, when the pilot attempted to retract airplane's landing gear, the gear would neither fully retract nor fully extend. The pilot attempted to extend the landing gear using the emergency manual extension hand pump. He reported the ". . .pump handle was locked solid and would not move. . ." He couldn't get the selector handle to recenter as it was supposed to and he didn't get a landing gear extended cockpit indication. The pilot elected to return to the departure airport. The pilot performed a flyby past the air traffic control tower and the controller radioed that all three gear appeared to be down; however, the pilot's wife, in the right seat, told him she couldn't see a wheel on that side of the airplane. During the ensuing landing, the right main landing gear collapsed, the right wing contacted the runway, and the airplane veered off the runway to the right. The aircraft was delivered for the annual inspection with a landing gear extension discrepancy. A misrigging problem on the left main landing gear seemed to explain all of the symptoms and was repaired. The gear was satisfactorily cycled 10 times using an external hydraulic pressure source (mule). Inspection subsequent to the accident revealed that, although functional, the output of the engine-driven hydraulic pump was deficient and insufficient to operate the gear. The emergency hand pump and emergency gear extension system operated normally. The maintenance facility manager speculated that the reason the pilot was not able to extend the landing gear with the emergency hand pump was because he didn't first fully extend the handle. If the telescoping handle shaft is not fully extended the handle cannot be moved and feels similar to a "hydraulic lock."
Probable Cause: The failure of maintenance personnel to properly diagnose the cause of a reported maintenance discrepancy resulting in the airplane being released from an annual inspection with a worn hydraulic pump which lacked sufficient output to operate the landing gear. Another cause was the pilot's improper execution of the landing gear emergency extension procedure by failing to fully extend the manual hydraulic pump handle prior to attempting emergency gear extension.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX02LA027 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB LAX02LA027
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 16:30 |
ASN Update Bot |
Added |
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