ASN Wikibase Occurrence # 298409
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Date: | Sunday 7 October 2001 |
Time: | 13:51 LT |
Type: | Worner 1000 STU |
Owner/operator: | Private |
Registration: | D-OAGH |
MSN: | 1069 |
Total airframe hrs: | 43 hours |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Liberal, Kansas -
United States of America
|
Phase: | Unknown |
Nature: | Demo/Airshow/Display |
Departure airport: | Albuquerque, NM |
Destination airport: | Liberal, KS |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot said their gas balloon was cruising at 3,000 feet agl over the Liberal, Kansas, area when they experienced a microburst. The pilot said they suddenly found themselves heading for the ground at a very high rate of descent. The pilot said they dropped ballast to try and slow their descent. He said he then saw that his angle of descent was going to take the balloon into power lines along a road. The pilot said he opened the vent and put the basket on the road. The envelope went into the power lines, tore open, caught fire, and burned. At the time of the accident the aviation routine weather report for Dodge City, Kansas, 60 miles northeast of the accident site, reported clear skies, 10 miles visibility, and winds of 180 degrees at 19 knots with gusts to 25 knots. The report also stated in the remarks that peak winds of 31 knots were recorded at 1600. The balloon was part of a gas balloon race associated with the annual Albuquerque Balloon Festival in which the contestants try to cover the farthest distance within a three day period.
Probable Cause: The pilot's inadvertent flight into adverse weather conditions during cruise flight and the unsuitable landing area encountered during the uncontrolled descent. Factors relating to this accident were the high wind, the pilot's unsuccessful attempt to compensate for the wind conditions, the pilot's unsuccessful attempt to avoid the power lines during the landing, and the power lines.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI02LA002 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB CHI02LA002
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 17:41 |
ASN Update Bot |
Added |
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