ASN Wikibase Occurrence # 298550
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 28 August 2001 |
Time: | 09:30 LT |
Type: | Bell 206-L4 |
Owner/operator: | Pacific Marine Leasing Inc. |
Registration: | N995PM |
MSN: | 52251 |
Year of manufacture: | 2000 |
Total airframe hrs: | 49 hours |
Engine model: | Allison 250-C3OP |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mesa, Arizona -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Mesa-Falcon Field, AZ (MSC/KFFZ) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During a practice autorotation, the helicopter landed hard bending the tail boom. An examination of the helicopter indicated the damage resulted from the hard landing. The tail boom had ripped out at the aft bulkhead, and the landing skids were bent upward at the aft end. The nose of the helicopter was also damaged when the helicopter rocked forward after the hard landing. The helicopter then stopped upright on the skids with no damage to the main rotor blades. The pilot stated that he was doing a practice autorotation landing when the accident occurred. During the last landing, the helicopter "fell through" much faster than anticipated. The pilot stated that no mechanical anomalies were experienced prior to or after the accident. The temperature at the time of the accident was 100 degrees Fahrenheit. The pilot stated that in the future he will allow a higher margin for autorotation power recovery in hot conditions.
Probable Cause: The pilot's improper autorotation in that he failed to attain the proper descent rate resulting in a hard landing and subsequent airframe damage. A factor was the high temperature.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX01LA292 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB LAX01LA292
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 19:21 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation