Accident Piper PA-32-300 N2116G,
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ASN Wikibase Occurrence # 298559
 
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Date:Sunday 26 August 2001
Time:08:56 LT
Type:Silhouette image of generic PA32 model; specific model in this crash may look slightly different    
Piper PA-32-300
Owner/operator:
Registration: N2116G
MSN: 32-7940015
Year of manufacture:1978
Total airframe hrs:2903 hours
Engine model:Lycoming IO-540-K1G5
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Homerville, GA -   United States of America
Phase: Unknown
Nature:Private
Departure airport:Kissimmee Gateway Airport, FL (ISM/KISM)
Destination airport:Lawrenceville-Gwinnett County Briscoe Field, GA (LZU/KLZU)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
Less than two hours into the flight, the engine lost power during cruise. During emergency descent, the airplane struck power lines and a tree, then collided with the ground. Examination of the engine accessory case revealed the idler gear was fractured, and the two attachment holes in the crank case for the idler gear shaft assembly were elongated. Three fractured teeth from the idler gear and two separated bolt heads were recovered. The fracture surface of each gear tooth displayed crack arrest marks and a rough surface consist with high-stress, low-cycle fatigue. The shanks below each separated bolt head were worn to about one-third their original diameter. The engine received a zero-time equivalent overhaul on May 9, 1985, and operated 1371 hours since the overhaul. Textron Lycoming Service Instruction No. 1009AQ states the recommended time between overhaul periods for the engine is 2000 hours. The Lycoming parts catalog for the engine specifies a bolt is required to attach the idler gear shaft assembly at one attachment hole, and a slotted nut and stud are required to attach the idler gear shaft assembly at the other attachment hole.

Probable Cause: The improper replacement of an accessory drive component with an unapproved part by maintenance personnel, which resulted in a fatigue fracture of the component and loss of engine power. The airplane subsequently collided with power lines and trees during an emergency landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL01LA095
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB ATL01LA095

Revision history:

Date/timeContributorUpdates
15-Oct-2022 19:27 ASN Update Bot Added
10-Nov-2022 17:30 Ron Averes Updated [Location, Narrative]

Corrections or additions? ... Edit this accident description

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