ASN Wikibase Occurrence # 298559
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Date: | Sunday 26 August 2001 |
Time: | 08:56 LT |
Type: | Piper PA-32-300 |
Owner/operator: | |
Registration: | N2116G |
MSN: | 32-7940015 |
Year of manufacture: | 1978 |
Total airframe hrs: | 2903 hours |
Engine model: | Lycoming IO-540-K1G5 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Homerville, GA -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Kissimmee Gateway Airport, FL (ISM/KISM) |
Destination airport: | Lawrenceville-Gwinnett County Briscoe Field, GA (LZU/KLZU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Less than two hours into the flight, the engine lost power during cruise. During emergency descent, the airplane struck power lines and a tree, then collided with the ground. Examination of the engine accessory case revealed the idler gear was fractured, and the two attachment holes in the crank case for the idler gear shaft assembly were elongated. Three fractured teeth from the idler gear and two separated bolt heads were recovered. The fracture surface of each gear tooth displayed crack arrest marks and a rough surface consist with high-stress, low-cycle fatigue. The shanks below each separated bolt head were worn to about one-third their original diameter. The engine received a zero-time equivalent overhaul on May 9, 1985, and operated 1371 hours since the overhaul. Textron Lycoming Service Instruction No. 1009AQ states the recommended time between overhaul periods for the engine is 2000 hours. The Lycoming parts catalog for the engine specifies a bolt is required to attach the idler gear shaft assembly at one attachment hole, and a slotted nut and stud are required to attach the idler gear shaft assembly at the other attachment hole.
Probable Cause: The improper replacement of an accessory drive component with an unapproved part by maintenance personnel, which resulted in a fatigue fracture of the component and loss of engine power. The airplane subsequently collided with power lines and trees during an emergency landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL01LA095 |
Status: | Investigation completed |
Duration: | |
Download report: | Final report |
|
Sources:
NTSB ATL01LA095
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 19:27 |
ASN Update Bot |
Added |
10-Nov-2022 17:30 |
Ron Averes |
Updated [Location, Narrative] |
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