ASN Wikibase Occurrence # 298560
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 25 August 2001 |
Time: | 14:35 LT |
Type: | Quickie Super Quickie 2 |
Owner/operator: | |
Registration: | N34DQ |
MSN: | SQ-01 |
Engine model: | Revmaster D-2100 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Bonney Lake, Washington -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | AUBURN, WA (S50) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that as he reduced the throttle, while in a descent, the engine quit. He attempted to restart the engine without success, and elected to make an off-airport landing. Post-accident inspection of the carburetor revealed that the carburetor was adjusted to an excessively lean mixture setting, precluding stable operation below 1500 RPM. The pilot reported that prior to the accident flight, he adjusted the carburetor in an effort to overcome an excessively rich mixture setting.
Probable Cause: Improper carburetor adjustment resulting in a total loss of engine power while in a descent configuration. Factors include an excessively lean mixture setting and unsuitable terrain for landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA01LA157 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB SEA01LA157
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 19:27 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation