ASN Wikibase Occurrence # 298570
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Date: | Thursday 23 August 2001 |
Time: | 15:45 LT |
Type: | Cessna 182R Skylane |
Owner/operator: | Civil Air Patrol |
Registration: | N5419E |
MSN: | 18268317 |
Year of manufacture: | 1983 |
Total airframe hrs: | 2672 hours |
Engine model: | Teledyne Cont O-470-U24B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Elizabethtown, KY -
United States of America
|
Phase: | Unknown |
Nature: | Ferry/positioning |
Departure airport: | Fort Knox-Godman AAF, KY (FTK/KFTK) |
Destination airport: | Elizabethtown Airport, KY (EKX/KEKX) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The Civil Air Patrol (CAP) pilot elected to make a flight with an inoperative right brake. He found that the brake was inoperative during his pre-flight inspection, from a write-up left by the previous pilot. He talked to the CAP wing maintenance officer, and together they agreed that the pilot would ferry the airplane to another airport for maintenance. He departed without incident. In the landing pattern at the destination airport, the pilot elected to land with a 10-knot quartering tailwind with no flaps. He was unable to stop the airplane on the 5,000-foot runway, and it ran off the departure end. The airplane went through a ditch, and came to rest inverted in a cornfield. An aluminum brake line attached to the right side tubular steel landing gear strut had chaffed against the aluminum covering over the strut, and developed a leak near the lower end of the strut. Dried hydraulic fluid was found inside the aluminum covering. The mechanic who performed the last inspection stated that he did not normally remove the aluminum fairings which were installed over the tubular steed landing gear strut.
Probable Cause: The pilot's improper decision to fly the airplane with a known deficiency, and his inflight decision to land with a quartering tailwind. A factor was the wing maintenance officer's concurrence to fly the airplane with the known deficiency.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC01LA216 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB NYC01LA216
History of this aircraft
Other occurrences involving this aircraft
6 May 2018 |
N5419E |
Civil Air Patrol |
0 |
Clarksville, TN |
|
sub |
Runway excursion |
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 19:34 |
ASN Update Bot |
Added |
01-Jun-2023 03:13 |
Ron Averes |
Updated |
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