ASN Wikibase Occurrence # 298704
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Date: | Wednesday 12 July 2000 |
Time: | 11:30 LT |
Type: | Aeronca 65-TC |
Owner/operator: | Private |
Registration: | N29416 |
MSN: | L3080T |
Total airframe hrs: | 2894 hours |
Engine model: | Continental A-65-8 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | HARRIS, North Carolina -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | , NC (NC02) |
Destination airport: | CAROLEEN , NC (8NC2) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot flew to a nearby airport, landed, remained on the ground with the engine running, then elected to depart. During the initial climb about 50-100 feet agl, the engine experienced a loss of power. Unable to maintain altitude he maneuvered towards a sandbar in a river and while descending to fly beneath a trestle bridge that was between his location and the sandbar, the airplane collided with a wire beneath the bridge. The airplane veered to the right, descended and impacted with 'scrub trees/saplings' on a side of the river. Examination of the airplane revealed 'rust' from a fuel line between the header tank and the fuel shut-off valve. Removal of the rust revealed an increase in fuel flow to the carburetor. Cold differential compression testing of each cylinder revealed no cylinder was greater than 52 psi when using 80 psi as a reference. The last annual inspection occurred on February 3, 2000; the airplane had accumulated approximately 20 hours since then. No inspections were recorded between a periodic inspection on June 8, 1963, and an annual inspection December 12, 1994. The December 1994 entry indicates, 'Assembled aircraft after long term storage....' No record of fuel lines was noted.
Probable Cause: The unsuitable terrain encountered by the pilot while descending for a forced landing. Contributing to the accident was the partial loss of engine power due a blocked fuel line resulting in fuel starvation.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA00LA220 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB MIA00LA220
Revision history:
Date/time | Contributor | Updates |
15-Oct-2022 21:38 |
ASN Update Bot |
Added |
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