Accident Mooney M20D N31M,
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ASN Wikibase Occurrence # 298897
 
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Date:Thursday 8 June 2000
Time:09:25 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20D
Owner/operator:Private
Registration: N31M
MSN: 188
Total airframe hrs:3523 hours
Engine model:Lycoming O-360
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Baker, California -   United States of America
Phase: Unknown
Nature:Private
Departure airport:GRAND JUNCTION, CO (GJT
Destination airport:BIG BEAR, CA (L35)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot collided with a sand dune after making a forced landing on a service road. It was during cruise flight when the pilot had first observed the fluctuation (a drop) on the fuel pressure indicator. He reported the same fluctuation after switching from the left tank to the right another hour into the flight. Activating the electric fuel pump had remedied the situation and it was left on for another hour. The fuel tanks were then switched again and the fuel pump was turned off. About 25 minutes had passed when the pressure dropped to zero and the engine lost power. The pilot tried various engine out procedures and to maneuver the airplane in an effort to get the engine to run, but his attempts to restart were unsuccessful. He had been receiving radar flight following service and declared an emergency before landing the airplane on a service road next to some railroad tracks. The left wing was torn and the right main gear had collapsed. The sheriff deputy who responded to the scene did not observe any fuel in the left tank and very minimal fuel in the right wing fuel tank. The deputy also reported the fuel gauges were indicating fuel on board when he turned the master switch on. A post crash inspection of the fuel selector body and screen revealed contamination in the system. The owner photographed the components, which displayed debris in the selector body below the fuel screen area. Both fuel tanks were resealed with a similar colored compound in December 1997. The last annual inspection was performed on the airplane in December 1999. The maintenance technician did not recollect any unusual contamination at the time.

Probable Cause: The fuel flow became restricted by remnants of fuel tank sealant that had accumulated in the fuel selector screen. Contributing to the pilot's inability to restart the engine in flight was the empty fuel tank in the left wing and the fuel gauge indication. The constrained landing area was also a factor.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX00LA222
Status: Investigation completed
Duration: 2 years and 6 months
Download report: Final report

Sources:

NTSB LAX00LA222

History of this aircraft

Other occurrences involving this aircraft
10 April 2021 N767DP Private 0 Los Angeles County, Palmdale, CA unk

Revision history:

Date/timeContributorUpdates
16-Oct-2022 00:00 ASN Update Bot Added

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