ASN Wikibase Occurrence # 298932
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Date: | Thursday 1 June 2000 |
Time: | 01:00 LT |
Type: | Piper PA-28-180 |
Owner/operator: | Claire Cheatham |
Registration: | N7271W |
MSN: | 28-1107 |
Year of manufacture: | 1963 |
Total airframe hrs: | 2680 hours |
Engine model: | Lycoming O-360-A3A |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | TULSA, Oklahoma -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | (KRVS) |
Destination airport: | COLORADO SPGS , CO (00V |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The private pilot stated that the airplane's preflight inspection and pre-takeoff engine run-up did not reveal any anomalies. The night cross-country flight departed from runway 01L and the airplane was climbing through 1,100 feet msl (463 feet agl) when the pilot noticed a hot smell and, subsequently, the engine lost total power. The pilot attempted to find a landing area and the pilot-rated passenger, who was a certified flight instructor (CFI), attempted to re-start the engine; however, the engine did not re-start. The pilot then relinquished control of the airplane to the CFI and a forced landing was executed. During the forced landing, the airplane impacted a tree and came to a stop upright. A pilot-rated witness added that he heard the airplane's engine 'missing badly,' during the initial takeoff climb. The airframe and engine logbooks were examined and no open maintenance discrepancies were noted. The reason for the loss of engine power was not determined during the airframe examination or engine test run.
Probable Cause: the loss of engine power for an undetermined reason. A contributing factor was the lack of suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW00LA163 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB FTW00LA163
Revision history:
Date/time | Contributor | Updates |
16-Oct-2022 00:29 |
ASN Update Bot |
Added |
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