ASN Wikibase Occurrence # 298951
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Date: | Saturday 27 May 2000 |
Time: | 09:29 LT |
Type: | Cessna 150L |
Owner/operator: | Kaz-air-inc. |
Registration: | N330JC |
MSN: | 15075400 |
Year of manufacture: | 1973 |
Engine model: | Continental O-200A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | MILLEDGEVILLE, Georgia -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | (KMLJ) |
Destination airport: | PINE MOUNTAIN , GA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The fuel tanks were full and a minimum of 22.5 pounds of cargo was on-board. The airplane was approximately 14 pounds over gross weight at the time of the accident. The pilot performed an engine run-up; no discrepancies were noted. The pilot noted that at rotation speed, the, '...aircraft seemed a little more sluggish then on our approach....' The pilot pitched for best rate of climb (70 mph), and continued in a slight climb. The stall warning horn sounded when the flight was near the end of the runway and again while flying over trees. The pilot verified throttle, mixture, and flap positions. He banked to the left to maneuver the airplane and it, '...immediately went into a full stall and rolled over the left wing....' The came to rest inverted in a ditch with water. The pilot did not report a loss of engine power in his report or to the operator of the airplane. Postaccident, the engine was started and operated to 1,200 to 1,500 rpm, impact damage precluded operation at a higher rpm. The left magneto was deemed inoperative but bench tested satisfactory. No fuel contamination of the fueling facility was noted.
Probable Cause: The operation of the airplane by the pilot-in-command in an over gross weight condition, the failure of the pilot to maintain airspeed (Vs) after takeoff, and the intentional stalling of the airplane by the pilot-in-command for his attempting to bank while flying close to stall airspeed.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA00LA174 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB MIA00LA174
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
16-Oct-2022 00:41 |
ASN Update Bot |
Added |
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