Fuel exhaustion Accident Zenith STOL CH 701 N942PS,
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ASN Wikibase Occurrence # 298997
 
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Date:Sunday 14 May 2000
Time:18:45 LT
Type:Silhouette image of generic CH70 model; specific model in this crash may look slightly different    
Zenith STOL CH 701
Owner/operator:Private
Registration: N942PS
MSN: 7-1568
Total airframe hrs:444 hours
Engine model:Rotax 582UL
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:WAKE FORREST, North Carolina -   United States of America
Phase: Unknown
Nature:Private
Departure airport:KNIGHTDALE , NC
Destination airport:WAKE FORREST , NC (NA
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot was conducting a cross country flight with several intermediate stops. He was in cruise flight at 1,500 feet on the last leg of the flight when the airplane sustained a reduction in engine power. He started a left 360-degree turn in preparation for a forced landing, the engine power came back and decreased again. At the 180-degree point in the turn he observed a better forced landing area, he lowered the nose and the power increased again. He reduced the power to the idle position, turned the ignition switch off, applied flaps and started a left slip in order to reach the forced landing area. The airplane was fast and he was concerned about trees at the edge of the forced landing area. He forced the airplane onto the ground hard separating the landing gear, the airplane turned to the left and the right wing tip collided with the ground. Examination of the fuel tank by the pilot revealed no fuel was present in the fuel tank. The pilot stated the fuel burn was this flight was significantly higher than the projected burn which caused the engine to die from fuel starvation.

Probable Cause: The pilot's improper fuel management during a cross country flight resulting in a loss of engine power due to fuel exhaustion, and his failure to achieve the proper touchdown point during a forced landing. This resulted in the pilot forcing the airplane onto the ground hard, and subsequent separation of the landing gear.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA00LA156
Status: Investigation completed
Duration: 6 months
Download report: Final report

Sources:

NTSB MIA00LA156

History of this aircraft

Other occurrences involving this aircraft
3 March 1993 N942PS Private 0 Durham, ME sub

Revision history:

Date/timeContributorUpdates
16-Oct-2022 01:17 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

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