Accident Cessna 310C N3311H,
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ASN Wikibase Occurrence # 299210
 
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Date:Wednesday 22 March 2000
Time:16:30 LT
Type:Silhouette image of generic C310 model; specific model in this crash may look slightly different    
Cessna 310C
Owner/operator:Leon Matheson
Registration: N3311H
MSN: 35835
Year of manufacture:1954
Engine model:Continental IO-470-D
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:CEDAR CITY, Utah -   United States of America
Phase: Unknown
Nature:Training
Departure airport:(KCDC)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight instructor said that he shut down the right engine to practice single engine flight. Attempts to restart the engine were unsuccessful (it was later determined that the mixture control cable had failed). The pilot did not feather the right engine, and he reported that the left engine was providing insufficient power to maintain flight. The flight instructor performed a gear down landing in the rough, brush covered desert. The owner of the airplane said that the practice engine shut down was performed at 9,500 feet mean sea level, or approximately 3,800 feet above the terrain. He said that the practice maneuver was not initiated over a landing airfield, but that two were available within 5 miles of this location. The airplane's Owner's Manual performance section indicates that the single engine best rate of climb would be from 50 feet per minute to 250 feet per minute, depending on altitude and outside air temperature. A manufacturer's representative said that a non-feathered propeller would reduce the rate of climb by approximately 400 feet per minute, and landing gear extended would reduce it an additional 300 feet per minute.

Probable Cause: The failure of the right engine mixture control cable, which prevented the pilot from restarting the engine. Contributing factors were the pilot's failure to follow procedures by not feathering the right propeller, the rough terrain, and the high vegetation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: DEN00LA066
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB DEN00LA066

Revision history:

Date/timeContributorUpdates
16-Oct-2022 03:53 ASN Update Bot Added

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