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Date: | Friday 28 January 2000 |
Time: | 21:30 LT |
Type: | Fairchild SA227-AT Expediter |
Owner/operator: | Ameriflight |
Registration: | N245DH |
MSN: | AT-624-B |
Year of manufacture: | 1985 |
Total airframe hrs: | 14251 hours |
Engine model: | Garrett TPE331 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | FAYETTEVILLE, Arkansas -
United States of America
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | TULSA , OK (KTUL) |
Destination airport: | (KFYV) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:On departure for the night air taxi cargo flight, the flight crew experienced a problem with the crew intercom system. The crew initiated their descent at a 'later than normal distance' from the airport, and as a result, a power reduction below 25 percent torque was required, which set off the gear warning horn. The sound 'eventually became part of the background noise.' During the approach, the captain asked the tower to dim the runway lights. At that time, the runway and approach lights went out and the crew lost sight of the runway. While the captain was asking the tower to turn the lights back on, the first officer called 'gear down, syncs off, speeds high, below the line check list.' The captain did not hear the first officer's callout and did not lower the landing gear. The captain stated that he did not hear the first officer's callout 'either because of the conversation [he] was having with the tower or because of the intercom system difficulties.' As the approach continued, the first officer had a problem slowing the airplane to proper approach speed. The airplane touched down on the runway with the landing gear retracted, 'slid' about 2,500 feet and exited the left side of the runway.
Probable Cause: The flight crew's failure to extend the landing gear. Contributing factors were the flight crew's non-compliance with the checklist, the pilot-in-command's diverted attention as a result of the loss of instrument approach/runway lighting, the partial failure of the instrument approach/runway lighting system, and the partial failure of the intercom system.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW00LA078 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB FTW00LA078
Revision history:
Date/time | Contributor | Updates |
16-Oct-2022 05:46 |
ASN Update Bot |
Added |
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