Accident Beechcraft E50 Twin Bonanza N4265R,
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ASN Wikibase Occurrence # 301081
 
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Date:Saturday 28 June 1997
Time:14:30 LT
Type:Silhouette image of generic BE50 model; specific model in this crash may look slightly different    
Beechcraft E50 Twin Bonanza
Owner/operator:Tennessee Skydiving Center
Registration: N4265R
MSN: LH-166
Total airframe hrs:14564 hours
Engine model:Lycoming O-480-1B
Fatalities:Fatalities: 0 / Occupants: 9
Aircraft damage: Substantial
Category:Accident
Location:TULLAHOMA, Tennessee -   United States of America
Phase: Unknown
Nature:Unknown
Departure airport:(KTHA)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The airplane was being used for sport parachute operations. During the initial climb after takeoff the right engine failed followed by the airplane's slow descending right turn into wooded terrain. The airplane crashed through trees and caught on fire. The fire was extinguished prior to the destruction of the airplane. Subsequent examination of the engine revealed that one crankshaft counterweight had broken its retaining lugs and was liberated inside the engine, resulting in sudden stoppage of the engine. The sudden stoppage prevented the pilot from feathering the propeller. Metallurgical examination of the crankshaft and counterweight revealed damage that was consistent with 'detuning' of the engine counterweights. Counterweight detuning results from excessively rapid throttle movements. Additionally, the engine log indicated that during an oil change 8 days before the accident, wear metal was found in the oil. The airplane continued to be flown with no further maintenance action taken.

Probable Cause: improper operation of the engine that produced internal damage, and improper servicing of the airplane by the owner/pilot mechanic that resulted in the subsequent mechanical failure of the engine crankshaft counterweight. Contributing to the accident was the pilot's inability to feather the propeller.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ATL97LA091
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB ATL97LA091

Revision history:

Date/timeContributorUpdates
13-Nov-2022 13:32 ASN Update Bot Added
18-Nov-2022 18:10 Ron Averes Updated [Aircraft type, Cn, Narrative]

Corrections or additions? ... Edit this accident description

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