ASN Wikibase Occurrence # 301095
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 17 December 1994 |
Time: | 16:00 LT |
Type: | Cessna 182A Skylane |
Owner/operator: | Skydive St. Louis |
Registration: | N6090B |
MSN: | 34090 |
Year of manufacture: | 1957 |
Total airframe hrs: | 6672 hours |
Engine model: | CONTINENTAL O-470-K |
Fatalities: | Fatalities: 0 / Occupants: 5 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | BOWLING GREEN, Missouri -
United States of America
|
Phase: | Unknown |
Nature: | Unknown |
Departure airport: | , MO (H19) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRPLANE TOOK OFF WITH FOUR PARACHUTISTS ON BOARD. AFTER REACHING AN ALTITUDE OF 11,000 FEET, ONE PARACHUTIST EXITED THE AIRPLANE. AS THE SECOND PARACHUTIST WAS EXITING, HIS RESERVE PARACHUTE DEPLOYED PULLING HIM TOWARD THE REAR OF THE AIRPLANE. THE PARACHUTE CANOPY WENT OVER THE TOP OF THE HORIZONTAL STABILIZER AND THE PARACHUTIST WENT UNDER THE STABILIZER. THE RESERVE PARACHUTE SUSPENSION LINES SLIPPED OFF THE HORIZONTAL STABILIZER. THE PARACHUTIST THEN OPENED THE MAIN PARACHUTE AND MADE A SUCCESSFUL DESCENT/LANDING. HOWEVER, THE STABILIZER AND EMPENNAGE WERE DAMAGED AND THE ELEVATOR WAS JAMMED. THE PILOT INSTRUCTED THE REMAINING PARACHUTISTS TO EXIT THE AIRPLANE. ALTHOUGH THE ELEVATOR WAS JAMMED, THE PILOT MANAGED TO LAND THE AIRPLANE IN A PLOWED CORN FIELD USING POWER AND AILERON CONTROL. DURING THE LANDING, THE AIRPLANE'S LANDING GEAR AND PROPELLER WERE DAMAGED. AN INVESTIGATION REVEALED EVIDENCE THAT THE DESIGN OF THE RESERVE PARACHUTE CABLE HOUSING WAS INADEQUATE (NOT ADEQUATELY SECURED), WHICH ALLOWED THE CABLE TO BE PULLED PREMATURELY. THE PARACHUTE MANUFACTURER (PARACHUTE INDUSTRY OF SOUTH AFRICA) AGREED TO REDESIGN THE HOUSING.
Probable Cause: INADEQUATE DESIGN OF THE RESERVE PARACHUTE CABLE HOUSING, WHICH RESULTED IN AN INADVERTENT DEPLOYMENT OF THE PARACHUTE, AND SUBSEQUENT COLLISION WITH, AND JAMMING OF, THE AIRCRAFT'S HORIZONTAL STABILIZER, NECESSITATING A FORCED LANDING.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI95LA060 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB CHI95LA060
Revision history:
Date/time | Contributor | Updates |
13-Nov-2022 13:34 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation