Accident Hughes 269 N9692F,
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ASN Wikibase Occurrence # 30119
 
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Date:Wednesday 14 June 2000
Time:09:15
Type:Silhouette image of generic H269 model; specific model in this crash may look slightly different    
Hughes 269
Owner/operator:King Aviation Centers
Registration: N9692F
MSN: 200892
Year of manufacture:1980
Total airframe hrs:7451 hours
Engine model:Lycoming IO-360-D1A
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Newhall Pass, near Santa Clarita, California -   United States of America
Phase: Landing
Nature:Training
Departure airport:VNY
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The helicopter touched down on the downside portion of a hill, struck a tree, and became inverted. The purpose of the flight was to conduct a new hire checkout. The purpose of the landing was to retrieve a door that had come off in flight the day prior to the accident. During the approach for landing the new hire pilot performed a high and low reconnaissance of the area. This was to check for wind direction and verify the landing area was clear of obstructions. About 100 feet from the intended touchdown point, the wind changed direction and became a tailwind. He attempted to compensate for the loss of altitude by increasing power, but the engine did not have enough power. The helicopter was still controllable with full left rudder. The helicopter started to settle and the engine and rotor rpm were decaying. When the new hire attempted to fly down hill to regain rpm, he felt resistance on the controls, but did not recall the check pilot indicating that he was going to take the controls. The check pilot instructed the other pilot to verify his rpm and verbalized that he was taking the flight controls. He attempted to perform a low rpm recovery. He reduced the collective and rolled on the throttle. However, he noted that the throttle was already in the full on position. He attempted to recover rpm by moving the collective up and down to clear the ridgeline. The helicopter continued to settle and landed hard. No discrepancies were noted with engine power.
Probable Cause: Settling with power precipitated by a wind direction change during the approach to land sequence and the check pilot's delayed remedial action to correct the event. Factors in the accident were crew resource management coordination concerning flight control authority and unsuitable terrain for landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX00LA226
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20001212X21267&key=1
FAA register: 2. http://registry.faa.gov/aircraftinquiry/NNum_Results.aspx?NNumbertxt=9692F

Revision history:

Date/timeContributorUpdates
27-Sep-2008 01:00 ASN archive Added
29-Nov-2014 00:37 Dr. John Smith Updated [Time, Total fatalities, Total occupants, Other fatalities, Location, Country, Phase, Nature, Departure airport, Destination airport, Source, Damage, Narrative]
21-Dec-2016 19:16 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:20 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
12-Dec-2017 18:49 ASN Update Bot Updated [Operator, Departure airport, Destination airport, Source, Narrative]

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