ASN Wikibase Occurrence # 305880
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Date: | Sunday 15 January 2023 |
Time: | 11:30 LT |
Type: | Piper PA-28-180 Cherokee |
Owner/operator: | Christopher Cardoza |
Registration: | N9687J |
MSN: | 28-3863 |
Year of manufacture: | 1967 |
Total airframe hrs: | 3025 hours |
Engine model: | Lycoming O-360-A4A |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Diego-Montgomery-Gibbs Executive Airport (MYF/KMYF), CA -
United States of America
|
Phase: | Take off |
Nature: | Training |
Departure airport: | San Diego-Montgomery-Gibbs Executive Airport, CA (MYF/KMYF) |
Destination airport: | Torrance Airport, CA (TOA/KTOA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor reported that prior to his arrival, the student pilot conducted a preflight inspection of the airplane. The flight instructor then visually inspected the airplane and did not observe any anomalies. On the takeoff roll, with the student pilot at the controls, the left side of the engine cowling opened just after rotation. The flight instructor took control of the airplane and reduced the engine's power setting to relieve stress on the cowling and abort the take off. However, the flight instructor determined that “was not the solution,' applied full power to the engine and elected to initiate a turn toward an alternate runway. The airplane continued to descend and was unable to reach the alternate runway. The flight instructor landed the airplane in muddy terrain off the runway. During the landing roll, the airplane's right main landing gear separated, and the right wing impacted the surface, resulting in substantial damage to the fuselage and right wing. The flight instructor reported that there were no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Probable Cause: The flight instructor's failure to maintain altitude while maneuvering to another runway after the engine cowling opened shortly after takeoff. Contributing to the accident was the failure of both the student pilot and flight instructor to conduct an adequate preflight inspection.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR23LA091 |
Status: | Investigation completed |
Duration: | 1 month |
Download report: | Final report |
|
Sources:
NTSB WPR23LA091
FAA register:
https://registry.faa.gov/aircraftinquiry/Search/NNumberResult?NNumbertxt=9687J Location
Media:
Revision history:
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