Serious incident Cessna 400 Corvalis (LC41-550FG) N932AC,
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ASN Wikibase Occurrence # 309963
 
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Date:Tuesday 8 December 2015
Time:08:50 LT
Type:Silhouette image of generic COL4 model; specific model in this crash may look slightly different    
Cessna 400 Corvalis (LC41-550FG)
Owner/operator:Private
Registration: N932AC
MSN: 411021
Year of manufacture:2008
Total airframe hrs:1027 hours
Engine model:Continental TSIO-550-C
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Minor
Category:Serious incident
Location:Seal Beach, California -   United States of America
Phase: En route
Nature:Private
Departure airport:San Diego, CA (KMYG)
Destination airport:Long Beach Airport, CA (LGB/KLGB)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The commercial pilot reported that the engine started "missing" [running rough] just after departure but he corrected the condition by leaning the mixture. While in cruise the engine started "missing" again but smoothed out after he turned towards a nearby airport, at which point the pilot decided to continue to his destination. When approximately 4 miles away from his destination the engine started to run rough, then quit. The pilot made a forced landing in to an open area. The pilot stated that he did not perform a magneto check at any time after the engine began running rough.

Examination of the engine magnetos revealed that the left magneto gear washer and nylon washer had been installed in reverse order resulting in rapid bushing wear and excessive radial play of the distributor drive gear. This wear led to a migration of the internal timing in the left magneto that could have led to misfires or kickbacks during start that caused shock to the gear train and damaged one or more distributor gear teeth in the right magneto. Damage to one or more gear teeth led to a cascade of gear tooth fractures as the right magneto continued to operate. Eventually the right magneto drive gear decoupled from the engine resulting in cylinder 3 or 6 receiving a spark each time the points were opened during cam rotation, causing random ignition of the fuel-air mixture in those cylinders.

The pilot's failure to follow the Pilot's Operating Handbook guidance to check the operation of the individual left and right magnetos once the engine began running rough likely missed the opportunity to regain engine power utilizing the functional left magneto.

Probable Cause: Improper maintenance performed on the left magneto which led to a loss of engine power. Contributing to the incident was the pilot's failure to check the magnetos in flight in compliance with manufacturers guidance regarding rough running engine. The pilot's decision to continue the flight after experiencing the rough running engine contributed to the necessity for a forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR16IA044
Status: Investigation completed
Duration: 2 years and 9 months
Download report: Final report

Sources:

NTSB WPR16IA044

Location

Revision history:

Date/timeContributorUpdates
01-Apr-2023 13:37 ASN Update Bot Added

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