ASN Wikibase Occurrence # 311711
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Date: | Monday 21 September 2020 |
Time: | 15:50 LT |
Type: | Cessna 172RG |
Owner/operator: | Purdue Aviation LLC |
Registration: | N6330V |
MSN: | 172RG0628 |
Year of manufacture: | 1968 |
Total airframe hrs: | 10041 hours |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Lafayette, Indiana -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Lafayette-Purdue University Airport, IN (LAF/KLAF) |
Destination airport: | Lafayette, IN |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The flight instructor (CFI) and student were airborne for about 10 minutes, in straight and level flight, when they heard and felt a 'clunkâ followed by the sound of the landing gear pump running continuously. They attempted to lower the landing gear and it did not come down. They subsequently smelled a burning odor, which was assessed to be from the landing gear pump, so they pulled the landing gear circuit breaker. They followed the landing gear manual extension checklist and troubleshot the problem, but there was no pressure in the manual pump and the landing gear would not extend. The CFI then performed a low pass over the runway and tower personnel advised that the nose gear appeared down and both main landing gear appeared partially extended. The CFI then performed a gear up landing during which the left main landing gear collapsed, resulting in substantial damage to the left horizontal stabilizer spars and the rear bulkhead. The CFI surmised that the right main landing gear locked down during the flare.
The wreckage was examined, and the nose gear up hydraulic line was found failed. The line had separated from the compression fitting on one end, which resulted in a loss of hydraulic fluid. The manual pump in the landing gear system utilizes the same landing gear hydraulics as the normal extension system, so the loss of hydraulic fluid rendered it inoperable and made it unlikely for all the landing gear to extend and lock down. The failed hydraulic line was installed in the airplane in May, 1993, and had 6,776.2 total hours since installation.
The failed hydraulic line was replaced, the airplane was placed on jacks, and the landing gear was swung and functionally tested using both the normal extension/retraction procedures and the manual/emergency extension procedures. The gear operated normally with each procedure and no additional failures or leaks were noted.
Probable Cause: The separation failure of a landing gear system hydraulic line and its compression fitting during cruise flight, which resulted in a partial gear up landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN20CA416 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB CEN20CA416
History of this aircraft
Other occurrences involving this aircraft
17 May 2014 |
N6330V |
Lafayette Aviation Inc |
0 |
Purdue University Airport (KLAF), Lafayette, Indiana |
|
unk |
Location
Revision history:
Date/time | Contributor | Updates |
02-May-2023 10:42 |
ASN Update Bot |
Added |
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