ASN Wikibase Occurrence # 311842
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Thursday 9 September 2021 |
Time: | 13:45 LT |
Type: | Thatcher CX-4 |
Owner/operator: | Private |
Registration: | N306TA |
MSN: | CX159 |
Year of manufacture: | 2008 |
Total airframe hrs: | 359 hours |
Engine model: | Revmaster 2100D |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Marshalltown, Iowa -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Marshalltown, IA |
Destination airport: | Marshalltown, IA |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot stated that he visually inspected the airplane fuel quantity before the flight and estimated there was 6 gallons of fuel. He said there was enough fuel for the planned flight with a fuel consumption rate of 3.5 gallons/hour. After he flew to an airport to perform a touch-and-go landing, in addition to local area flying, he began a return flight to the departure airport. He then realized that the airplane fuel quantity gauge indicated a fuel consumption that was greater than he had planned. About 3 miles from the departure/destination airport, the fuel gauge indicated near empty, and the engine ceased operation. He said he restarted the engine, which operated for about 5 seconds and then quit again. The pilot performed a forced landing on a corn field, during which the airplane nosed over. The airplane sustained substantial damage that included damage to the fuselage, empennage, and both wings. The pilot said the loss of engine power was due to his overestimation of fuel quantity during his preflight of the airplane and the inaccuracy of the fuel gauge. The pilot said there was no mechanical malfunction or failure of the airplane that would have precluded normal operations.
Probable Cause: The pilot's failure to properly determine the correct fuel quantity during preflight inspection that resulted in a loss of engine power during approach due to fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CEN21LA419 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB CEN21LA419
Location
Revision history:
Date/time | Contributor | Updates |
03-May-2023 05:11 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation